Penistone rail accidents

The Penistone Area
Legend
MS&LR to Barnsley
MS&LR to Sheffield
Barnsley Junction
Huddersfield Junction
PENISTONE (joint station)
Penistone Viaduct
Bullhouse (curve & bridge)
LYR to Huddersfield
DUNFORD BRIDGE
Woodhead Tunnel (summit)
MS&LR to Manchester

Over the latter years of the 19th and early years of the 20th centuries Penistone in Yorkshire gained a name as an accident black-spot on Britain's railway network, indeed it could be said to hold the title of the worst accident black-spot in the country. The main line through the town was the Woodhead route of the Manchester, Sheffield and Lincolnshire Railway between Sheffield Victoria and Manchester, London Road. The line was heavily graded with a summit some 400 yards inside the eastern portal of the Woodhead tunnel.

Contents

Stephenson and the cow, 1845

In one of the promotional meetings for the Sheffield, Ashton-under-Lyne and Manchester Railway a local farmer asked George Stephenson "what would happen if one of your locomotives hit one of my cows." Stephenson is reputed to have replied in a very broad, almost incomprehensible Geordie (Newcastle area) accent, "I would'na gi much chance for the coo!" At that time, Penistone Station was set on the line just below the parish church, which was adjacent to the cattle market. (The station was moved to the present site with the opening of the line to Huddersfield).

On 6 October 1845, Stephenson's thoughts were put to the test. The evening train from Dunford Bridge to Sheffield was running down the gradient towards Penistone Station when the train met a cow which had escaped onto the railway track from the cattle market. The drover was unable to move it out of the way and the train hit the cow. The locomotive and coaches were derailed and damaged, the guard injured and passengers shaken but Stephenson was proven right; the cow was almost cut in two and killed on the spot.[1]

The accident took place on the line towards Dunford Bridge, somewhere in the Bullhouse area and was considered to be caused by "Cattle Drover's neglect".

The Bullhouse Bridge Accident, 1884

Bullhouse Bridge rail accident
Details
Date 16 July 1884
Location Bullhouse Bridge
Country England
Rail line Manchester, Sheffield and Lincolnshire Railway
Cause axle failure
Statistics
Trains 1
Deaths 24
List of UK rail accidents by year

The first major accident occurred on 16 July 1884, a few miles to the west of the town, near Bullhouse Colliery. The accident is often referred to as being at "Bullhouse Bridge", where the road to Huddersfield passes below the line. An express passenger train, the 12.30 p.m. from Manchester London Road to London King's Cross, with through carriages for Grimsby Docks in connection with the evening steamer sailing, had left Woodhead Tunnel and was gathering speed on the downhill gradient towards Penistone. As it entered the curve at Bullhouse, the driver felt the engine develop an uneasy roll, but before he could apply the brakes, he heard a crack. A driving wheel axle on the locomotive had snapped, and the resulting spread of the driving wheels distorted the track. The axle fracture was probably caused by metal fatigue. A horsebox coupled behind the engine was derailed but remained upright. The coupling between the horsebox and the following carriages failed, and they ran off the rails and down the embankment on the outside of the curve. In total 24 passengers were killed with a high proportion being women.[2]

The Barnsley Junction Accident, 1885

The second unfortunate incident took place on the other side of Penistone Station, between Huddersfield Junction and Barnsley Junction, within six months. On 1 January 1885 a special excursion train from stations in the Sheffield area to Liverpool (9 coaches) and Southport (9 coaches) was climbing towards Penistone. At the same time a train of empty coal wagons travelling in the opposite direction to return the wagons to collieries in South Yorkshire and North Nottinghamshire was descending the gradient and had just passed the Huddersfield Junction signal box when one of the wagons derailed. The driver of the locomotive applied his brakes and this wagon, Shireoaks No. 218, jumped forward and became buffer-locked with the wagon in front, Shireoaks No. 1, which also came off the rails, and struck the locomotive of the excursion. The wagon was brushed aside by the locomotive but rebounded after the first four of the excursion's carriages passed. The fifth, sixth and seventh carriages were wrecked and the following three were brought off the track. One person was killed in the accident and two others died as a result of amputations.

On examination, Shireoaks No. 218 wagon was found to have a fractured axle with two flaws in the metal, a problem again caused by metal fatigue. Unexpected catastrophic failure of axles (and wheels) was a problem on all railway vehicles at the time, owing to the lack of understanding of the causes, especially fatigue crack initiation and growth. Crack initiation was usually caused either by defects or poor design, with stress concentrations raising the local stress to failure. The small crack so created would then grow slowly under repeated loading from usage until the axle could no longer withstand imposed loads. (It was noted that the day of the Barnsley Junction accident was very cold and the ballast under the railway sleepers was frozen, increasing the loads on the wheels and axles.)

Although the Manchester, Sheffield and Lincolnshire railway could not be held directly responsible for this accident, the enquiry recommended more thorough inspection of all rolling stock.[3]

The Huddersfield Junction Accident, 1889

The next serious accident occurred four years later on 30 March, 1889. This was the day of the F.A. Cup Final. Preston North End, then considered the best team in the country, were due to play Wolverhampton Wanderers at Kennington Oval, and the University Boat Race was to take place over the Thames Tideway between Putney and Mortlake in London. The Manchester, Sheffield and Lincolnshire Railway ran an excursion with portions from Liverpool, Southport and Wigan to London, Kings Cross. Although it was not intended as a football excursion, many people from Lancashire took advantage of it to watch Preston play. The Southport portion of the train was joined to the main train from Liverpool at Warrington Central and the Wigan portion was picked up at Glazebrook. The completed train made its way over the Cheshire Lines Committee tracks to Godley Junction where a stop was made for Railway Clearing House checks. It departed 55 minutes late. The locomotive was Class 23 No. 188, a six-coupled locomotive, which was usually to be found on goods workings, but was regularly used on excursion traffic.

The train ran down the gradient towards Penistone station when the locomotive, having no leading wheels to guide it, jumped the points where the goods line diverged from the main line on the approach to the Huddersfield Junction signal box. The locomotive crew stood by their posts and applied the brakes. The coaches followed the locomotive into the "six-foot" ripping up some 25 yards of track. The tender capsized and became entangled in signal wires, the locomotive dug into the ballast and the front coach was totally smashed. Coaches two and three toppled onto their sides and the following three which were pulled round in different directions were left standing broadside against the first pair. One person was killed and many injured.[4] Those with minor injuries were treated at Penistone Station, those with more severe injuries were taken to the Wentworth Arms Hotel, opposite the bottom of the station approach road, where the billiard room was turned into an operating theatre.

A further crash was averted by the prompt action of the signalman in Huddersfield Junction box. Having witnessed the crash he sent the message to Barnsley Junction, the next box on the Sheffield side, to "Stop the Mail", but the 10.40 p.m. King's Cross to Manchester Mail had already passed by. He set all his signals against the train and the driver applied his brakes but it could not stop before hitting the tender of the crashed locomotive. The Mail train's buffers penetrated the plating of the tender and the bogie wheels were thrown off the track, but the engine did not reach the crashed coaches.

The Railway Inspectorate found that the leading axle of the locomotive had fractured and questioned both the use of a "goods locomotive" on passenger work, where they would travel at higher speeds than usual, and the locomotive having no leading bogie wheels.

More 19th century accidents

8 December, 1882. An accident in Penistone station during shunting operations. Two passengers injured.

1 September, 1886. The through coach to Huddersfield, conveyed on the 5.30 p.m. King's Cross to Manchester (London Road) express was detached at Penistone and placed to await collection by the local train. The M.S.& L. locomotive and the leading brake backed onto its train, the impact sending the six coaches, dining car and rear brake into the ticket platform. Twenty passengers were slightly injured.[5]

September, 1887. Just one year later, an almost identical accident occurred.

10 October, 1897. An accident at Penistone station when a light locomotive collided with a carriage. Three people were injured, one later died of concussion.[6]

20th century accidents

2 February, 1916. Probably the only accident to take place on the Lancashire and Yorkshire Railway line, at the Penistone end of the viaduct which takes the tracks northward from the station. A Lancashire & Yorkshire Railway 2-4-2T locomotive, No. 661, was standing when the end of the viaduct and the embankment subsided below it. The collapse was slow and the crew jumped to safety before the arch fell down. The cause of the collapse was stated to be scouring of the foundations after prolonged heavy rain; the parapet of the viaduct had been observed to be cracked some days earlier.[7]

27 February, 1927. An avoidable accident blamed mainly on signalman's error, in which an L.M.S. locomotive, Aspinall radial tank No. 10760, from the Huddersfield line, having arrived and discharged its passengers, needed to clear the line to allow an empty coaching stock train from Bradford to enter the station. It shunted its stock into the other L.M.S. platform to prepare for the return working. The locomotive then needed to be turned (unnecessarily but following usual practice on the line) and worked to the opposite end of the train, a move needing quite a few backwards and forwards shunts. The final move to reach the front of his train was via the L.M.S. "up" line, a wrong line movement which started on the L.N.E.R. line as this was the only route available to reach his train. The driver made this last movement on his own, the fireman being sent to "mash" (brew) the tea in the porter's room. The last move was controlled by a hand signal but having given the signal, the Huddersfield Junction signalman, new on shift at 6 p.m., forgot to set the points for the L.M.S. line and the locomotive went along the main line into the station platform. The driver realised that something was wrong and stopped. On seeing the signal at the east end of the platform go "off", he thought that the signalman had realised his error and the signal was meant for him. He moved off to regain his right line, but the signal was in fact intended for the Manchester - Marylebone express, loaded to five coaches and hauled by class D10 "Director" No.5437 "Prince George", which was approaching. Because of the speed restriction in force at Penistone, the train was easing up and the impact speed was around 20 m.p.h. The L.M.S. driver was the most seriously hurt in the accident. His fireman jumped clear and the L.N.E.R. crew were shaken.

The Huddersfield Junction signalman was held to be responsible for the accident, although the L.M.S. driver did receive a mention in the report for his breach of rules. The Inspector also referred to Rule 55(b) which provided that the fireman should go to the signalbox and remain there to remind the signalman of the presence of his train, standing on a running line.

Effects on the railway

The stretch of line where all these accidents occurred is among some of the bleakest scenery in the Pennines, and as none of the earlier accidents could be conveniently ascribed to human error, the superstitious had a field day. Penistone was reckoned to be an unlucky place to cross the hills.[8] (Other folklore concerned the dangers of asphyxiation if a passenger train were to stall in the Woodhead Tunnels.) All these irrational beliefs hit the Manchester, Sheffield and Lincolnshire Railway hard.

After another accident at Hexthorpe near Doncaster in South Yorkshire in 1886, the workers of the M.S. & L. Railway offered to contribute a day's wages to help cover the costs resulting from the accident. The Board of the Railway declined this generous offer, considering it unfair to their workers.[9]

The Trans-Pennine rail route of the Manchester, Sheffield and Lincolnshire Railway is now part of the central section of the Trans-Pennine Trail.

See also

Notes

  1. ^ Dow vol. 1, p.52
  2. ^ Dow vol. 2, pp.199-200
  3. ^ Dow vol. 2, pp.200,202
  4. ^ Dow vol. 2, p.205
  5. ^ Dow vol. 2, p.202
  6. ^ Dow vol. 2, p.310
  7. ^ Marshall, p. 243
  8. ^ Dow vol. 2, p.202
  9. ^ Dow vol. 2, pp.202,204-205

Sources